Analysis Heat Exchanger Network Steam Power Plant in Using Pinch (Case Study in PT POMI Unit 3 Power Plant Paiton)

Rudiyanto, Bayu and Raga, Titah and Prasetyo, Totok and Rahmanto, Dedi and Nuruddin, Mochammad and Pambudi, Nugroho and Wibowo, Kukuh (2020) Analysis Heat Exchanger Network Steam Power Plant in Using Pinch (Case Study in PT POMI Unit 3 Power Plant Paiton). International Journal of Heat and Technology, 38 (2). pp. 439-446. ISSN 03928764

[img] Text (Hasil Cek Similarity)
6.pdf - Supplemental Material
Available under License Creative Commons Attribution Share Alike.

Download (2MB)
[img] Text (Hasil Peer Review)
47 - Hasil Peer Review.pdf - Supplemental Material
Restricted to Repository staff only

Download (1MB)
Official URL: http://www.iieta.org/journals/ijht/paper/10.18280/...

Abstract

PT. POMI Paiton Unit 3 is one of big steam power plant in Indonesia that provideelectricity with a capacity of 1 x 815 MW. This power plant requires a large amount ofcoal to produce electricity with a lot of large quantities, estimates of the total consume coalamounted to 3.06 million tons / year. The performance of the power plant PT. POMI Unit3 can be optimized by modifying the Heat Exchanger Network (HEN). Pinch method isused to optimize HEN, this method provides a good opportunity in the design or inevaluating HEN system. Research has been carried capable increase efficiency of 0.5% ofthe power plant that was originally 28.45% to 28.95%, and can reduce fuel use by 1.71 kg/ s initially as much as 97.99 kg / s to 96.28 kg / s, and can also be reconstructed from there-arrangement of Heat Exchanger Network of Power Plant PT. POMI Unit 3 Paiton.

Item Type: Article
Subjects: 410 - Rumpun Ilmu Teknik > 430 - Ilmu Keteknikan Industri > 443 - Teknik Enerji
Divisions: Kepegawaian
Depositing User: Bayu Rudiyanto
Date Deposited: 08 Mar 2021 09:00
Last Modified: 08 Apr 2021 09:55
URI: https://sipora.polije.ac.id/id/eprint/47

Actions (login required)

View Item View Item